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An evaluation of krypton propellant in Hall thrusters

Posted on:2008-06-22Degree:Ph.DType:Thesis
University:University of MichiganCandidate:Linnell, Jesse AllenFull Text:PDF
GTID:2442390005973654Subject:Engineering
Abstract/Summary:
Due to its high specific impulse and low price, krypton has long sparked interest as an alternate Hall thruster propellant. Unfortunately at the moment, krypton's relatively poor performance precludes it as a legitimate option. This thesis presents a detailed investigation into krypton operation in Hall thrusters. These findings suggest that the performance gap can be decreased to 4% and krypton can finally become a realistic propellant option.; Although krypton has demonstrated superior specific impulse, the xenon-krypton absolute efficiency gap ranges between 2 and 15%. A phenomenological performance model indicates that the main contributors to the efficiency gap are propellant utilization and beam divergence. Propellant utilization and beam divergence have relative efficiency deficits of 5 and 8%, respectively.; A detailed characterization of internal phenomena is conducted to better understand the xenon-krypton efficiency gap. Krypton's large beam divergence is found to be related to a defocusing equipotential structure and a weaker magnetic field topology. Ionization processes are shown to be linked to the Hall current, the magnetic mirror topology, and the perpendicular gradient of the magnetic field.; Several thruster design and operational suggestions are made to optimize krypton efficiency. Krypton performance is optimized for discharge voltages above 500 V and flow rates corresponding to an a greater than 0.015 mg/(mm-s), where alpha is a function of flow rate and discharge channel dimensions (alpha = m˙alphab/Ach). Performance can be further improved by increasing channel length or decreasing channel width for a given flow rate. Also, several magnetic field design suggestions are made to enhance ionization and beam focusing.; Several findings are presented that improve the understanding of general Hall thruster physics. Excellent agreement is shown between equipotential lines and magnetic field lines. The trim coil is shown to enhance beam focusing, ionization processes, and electron dynamics. Electron mobility and the Hall parameter are studied and compared to different mobility models. Azimuthal electron current is studied using a fluid and particle drift approach. Analyses of several magnetic field features are conducted and simple tools are suggested for the development of future Hall thrusters. These findings have strong implications for future Hall thruster design, lifetimes, and modeling.
Keywords/Search Tags:Hall, Krypton, Propellant, Magnetic field
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